VIRQs come in 3 flavors, per-VPU, per-domain, and global, and the VIRQs
are tracked in per-cpu virq_to_irq arrays.
Per-domain and global VIRQs must be bound on CPU 0, and
bind_virq_to_irq() sets the per_cpu virq_to_irq at registration time
Later, the interrupt can migrate, and info->cpu is updated. When
calling __unbind_from_irq(), the per-cpu virq_to_irq is cleared for a
different cpu. If bind_virq_to_irq() is called again with CPU 0, the
stale irq is returned. There won't be any irq_info for the irq, so
things break.
Make xen_rebind_evtchn_to_cpu() update the per_cpu virq_to_irq mappings
to keep them update to date with the current cpu. This ensures the
correct virq_to_irq is cleared in __unbind_from_irq().
Fixes: e46cdb66c8fc ("xen: event channels")
Cc: stable(a)vger.kernel.org
Signed-off-by: Jason Andryuk <jason.andryuk(a)amd.com>
---
v3:
Kernel style brace placement
Delay setting old_cpu and tighten scope of variable
v2:
Different approach changing virq_to_irq
---
drivers/xen/events/events_base.c | 13 ++++++++++++-
1 file changed, 12 insertions(+), 1 deletion(-)
diff --git a/drivers/xen/events/events_base.c b/drivers/xen/events/events_base.c
index b060b5a95f45..9478fae014e5 100644
--- a/drivers/xen/events/events_base.c
+++ b/drivers/xen/events/events_base.c
@@ -1797,9 +1797,20 @@ static int xen_rebind_evtchn_to_cpu(struct irq_info *info, unsigned int tcpu)
* virq or IPI channel, which don't actually need to be rebound. Ignore
* it, but don't do the xenlinux-level rebind in that case.
*/
- if (HYPERVISOR_event_channel_op(EVTCHNOP_bind_vcpu, &bind_vcpu) >= 0)
+ if (HYPERVISOR_event_channel_op(EVTCHNOP_bind_vcpu, &bind_vcpu) >= 0) {
+ int old_cpu = info->cpu;
+
bind_evtchn_to_cpu(info, tcpu, false);
+ if (info->type == IRQT_VIRQ) {
+ int virq = info->u.virq;
+ int irq = per_cpu(virq_to_irq, old_cpu)[virq];
+
+ per_cpu(virq_to_irq, old_cpu)[virq] = -1;
+ per_cpu(virq_to_irq, tcpu)[virq] = irq;
+ }
+ }
+
do_unmask(info, EVT_MASK_REASON_TEMPORARY);
return 0;
--
2.34.1
Change find_virq() to return -EEXIST when a VIRQ is bound to a
different CPU than the one passed in. With that, remove the BUG_ON()
from bind_virq_to_irq() to propogate the error upwards.
Some VIRQs are per-cpu, but others are per-domain or global. Those must
be bound to CPU0 and can then migrate elsewhere. The lookup for
per-domain and global will probably fail when migrated off CPU 0,
especially when the current CPU is tracked. This now returns -EEXIST
instead of BUG_ON().
A second call to bind a per-domain or global VIRQ is not expected, but
make it non-fatal to avoid trying to look up the irq, since we don't
know which per_cpu(virq_to_irq) it will be in.
Cc: stable(a)vger.kernel.org
Signed-off-by: Jason Andryuk <jason.andryuk(a)amd.com>
---
v3:
Cc: stable as a pre-req for the subsequent virg tracking change
Call __unbind_from_irq() on error ro avoid leaking info
v2:
New
---
drivers/xen/events/events_base.c | 19 ++++++++++++++-----
1 file changed, 14 insertions(+), 5 deletions(-)
diff --git a/drivers/xen/events/events_base.c b/drivers/xen/events/events_base.c
index 374231d84e4f..b060b5a95f45 100644
--- a/drivers/xen/events/events_base.c
+++ b/drivers/xen/events/events_base.c
@@ -1314,10 +1314,12 @@ int bind_interdomain_evtchn_to_irq_lateeoi(struct xenbus_device *dev,
}
EXPORT_SYMBOL_GPL(bind_interdomain_evtchn_to_irq_lateeoi);
-static int find_virq(unsigned int virq, unsigned int cpu, evtchn_port_t *evtchn)
+static int find_virq(unsigned int virq, unsigned int cpu, evtchn_port_t *evtchn,
+ bool percpu)
{
struct evtchn_status status;
evtchn_port_t port;
+ bool exists = false;
memset(&status, 0, sizeof(status));
for (port = 0; port < xen_evtchn_max_channels(); port++) {
@@ -1330,12 +1332,16 @@ static int find_virq(unsigned int virq, unsigned int cpu, evtchn_port_t *evtchn)
continue;
if (status.status != EVTCHNSTAT_virq)
continue;
- if (status.u.virq == virq && status.vcpu == xen_vcpu_nr(cpu)) {
+ if (status.u.virq != virq)
+ continue;
+ if (status.vcpu == xen_vcpu_nr(cpu)) {
*evtchn = port;
return 0;
+ } else if (!percpu) {
+ exists = true;
}
}
- return -ENOENT;
+ return exists ? -EEXIST : -ENOENT;
}
/**
@@ -1382,8 +1388,11 @@ int bind_virq_to_irq(unsigned int virq, unsigned int cpu, bool percpu)
evtchn = bind_virq.port;
else {
if (ret == -EEXIST)
- ret = find_virq(virq, cpu, &evtchn);
- BUG_ON(ret < 0);
+ ret = find_virq(virq, cpu, &evtchn, percpu);
+ if (ret) {
+ __unbind_from_irq(info, info->irq);
+ goto out;
+ }
}
ret = xen_irq_info_virq_setup(info, cpu, evtchn, virq);
--
2.34.1
Testing has shown that reading multiple registers at once (for 10-bit
ADC values) does not work. Set the use_single_read regmap_config flag
to make regmap split these for us.
This should fix temperature opregion accesses done by
drivers/acpi/pmic/intel_pmic_chtdc_ti.c and is also necessary for
the upcoming drivers for the ADC and battery MFD cells.
Fixes: 6bac0606fdba ("mfd: Add support for Cherry Trail Dollar Cove TI PMIC")
Cc: stable(a)vger.kernel.org
Reviewed-by: Andy Shevchenko <andy(a)kernel.org>
Signed-off-by: Hans de Goede <hansg(a)kernel.org>
---
Changes in v3:
- Fix a few typos in the commit message
Changes in v2:
- Update comment to: "The hardware does not support reading multiple
registers at once"
---
drivers/mfd/intel_soc_pmic_chtdc_ti.c | 2 ++
1 file changed, 2 insertions(+)
diff --git a/drivers/mfd/intel_soc_pmic_chtdc_ti.c b/drivers/mfd/intel_soc_pmic_chtdc_ti.c
index 4c1a68c9f575..6daf33e07ea0 100644
--- a/drivers/mfd/intel_soc_pmic_chtdc_ti.c
+++ b/drivers/mfd/intel_soc_pmic_chtdc_ti.c
@@ -82,6 +82,8 @@ static const struct regmap_config chtdc_ti_regmap_config = {
.reg_bits = 8,
.val_bits = 8,
.max_register = 0xff,
+ /* The hardware does not support reading multiple registers at once */
+ .use_single_read = true,
};
static const struct regmap_irq chtdc_ti_irqs[] = {
--
2.49.0
When the host actively triggers SSR and collects coredump data,
the Bluetooth stack sends a reset command to the controller. However, due
to the inability to clear the QCA_SSR_TRIGGERED and QCA_IBS_DISABLED bits,
the reset command times out.
To address this, this patch clears the QCA_SSR_TRIGGERED and
QCA_IBS_DISABLED flags and adds a 50ms delay after SSR, but only when
HCI_QUIRK_NON_PERSISTENT_SETUP is not set. This ensures the controller
completes the SSR process when BT_EN is always high due to hardware.
For the purpose of HCI_QUIRK_NON_PERSISTENT_SETUP, please refer to
the comment in `include/net/bluetooth/hci.h`.
The HCI_QUIRK_NON_PERSISTENT_SETUP quirk is associated with BT_EN,
and its presence can be used to determine whether BT_EN is defined in DTS.
After SSR, host will not download the firmware, causing
controller to remain in the IBS_WAKE state. Host needs
to synchronize with the controller to maintain proper operation.
Multiple triggers of SSR only first generate coredump file,
due to memcoredump_flag no clear.
add clear coredump flag when ssr completed.
When the SSR duration exceeds 2 seconds, it triggers
host tx_idle_timeout, which sets host TX state to sleep. due to the
hardware pulling up bt_en, the firmware is not downloaded after the SSR.
As a result, the controller does not enter sleep mode. Consequently,
when the host sends a command afterward, it sends 0xFD to the controller,
but the controller does not respond, leading to a command timeout.
So reset tx_idle_timer after SSR to prevent host enter TX IBS_Sleep mode.
Changes since v6-7:
- Merge the changes into a single patch.
- Update commit.
Changes since v1-5:
- Add an explanation for HCI_QUIRK_NON_PERSISTENT_SETUP.
- Add commments for msleep(50).
- Update format and commit.
Signed-off-by: Shuai Zhang <quic_shuaz(a)quicinc.com>
---
drivers/bluetooth/hci_qca.c | 33 +++++++++++++++++++++++++++++++++
1 file changed, 33 insertions(+)
diff --git a/drivers/bluetooth/hci_qca.c b/drivers/bluetooth/hci_qca.c
index 4e56782b0..9dc59b002 100644
--- a/drivers/bluetooth/hci_qca.c
+++ b/drivers/bluetooth/hci_qca.c
@@ -1653,6 +1653,39 @@ static void qca_hw_error(struct hci_dev *hdev, u8 code)
skb_queue_purge(&qca->rx_memdump_q);
}
+ /*
+ * If the BT chip's bt_en pin is connected to a 3.3V power supply via
+ * hardware and always stays high, driver cannot control the bt_en pin.
+ * As a result, during SSR (SubSystem Restart), QCA_SSR_TRIGGERED and
+ * QCA_IBS_DISABLED flags cannot be cleared, which leads to a reset
+ * command timeout.
+ * Add an msleep delay to ensure controller completes the SSR process.
+ *
+ * Host will not download the firmware after SSR, controller to remain
+ * in the IBS_WAKE state, and the host needs to synchronize with it
+ *
+ * Since the bluetooth chip has been reset, clear the memdump state.
+ */
+ if (!test_bit(HCI_QUIRK_NON_PERSISTENT_SETUP, &hdev->quirks)) {
+ /*
+ * When the SSR (SubSystem Restart) duration exceeds 2 seconds,
+ * it triggers host tx_idle_delay, which sets host TX state
+ * to sleep. Reset tx_idle_timer after SSR to prevent
+ * host enter TX IBS_Sleep mode.
+ */
+ mod_timer(&qca->tx_idle_timer, jiffies +
+ msecs_to_jiffies(qca->tx_idle_delay));
+
+ /* Controller reset completion time is 50ms */
+ msleep(50);
+
+ clear_bit(QCA_SSR_TRIGGERED, &qca->flags);
+ clear_bit(QCA_IBS_DISABLED, &qca->flags);
+
+ qca->tx_ibs_state = HCI_IBS_TX_AWAKE;
+ qca->memdump_state = QCA_MEMDUMP_IDLE;
+ }
+
clear_bit(QCA_HW_ERROR_EVENT, &qca->flags);
}
--
2.34.1
From: Conor Dooley <conor.dooley(a)microchip.com>
In commit 13529647743d9 ("spi: microchip-core-qspi: Support per spi-mem
operation frequency switches") the logic for checking the viability of
op->max_freq in mchp_coreqspi_setup_clock() was copied into
mchp_coreqspi_supports_op(). Unfortunately, op->max_freq is not valid
when this function is called during probe but is instead zero.
Accordingly, baud_rate_val is calculated to be INT_MAX due to division
by zero, causing probe of the attached memory device to fail.
Seemingly spi-microchip-core-qspi was the only driver that had such a
modification made to its supports_op callback when the per_op_freq
capability was added, so just remove it to restore prior functionality.
CC: stable(a)vger.kernel.org
Reported-by: Valentina Fernandez <valentina.fernandezalanis(a)microchip.com>
Fixes: 13529647743d9 ("spi: microchip-core-qspi: Support per spi-mem operation frequency switches")
Signed-off-by: Conor Dooley <conor.dooley(a)microchip.com>
---
CC: Conor Dooley <conor.dooley(a)microchip.com>
CC: Daire McNamara <daire.mcnamara(a)microchip.com>
CC: Mark Brown <broonie(a)kernel.org>
CC: Miquel Raynal <miquel.raynal(a)bootlin.com>
CC: linux-spi(a)vger.kernel.org
CC: linux-kernel(a)vger.kernel.org
---
drivers/spi/spi-microchip-core-qspi.c | 12 ------------
1 file changed, 12 deletions(-)
diff --git a/drivers/spi/spi-microchip-core-qspi.c b/drivers/spi/spi-microchip-core-qspi.c
index d13a9b755c7f8..8dc98b17f77b5 100644
--- a/drivers/spi/spi-microchip-core-qspi.c
+++ b/drivers/spi/spi-microchip-core-qspi.c
@@ -531,10 +531,6 @@ static int mchp_coreqspi_exec_op(struct spi_mem *mem, const struct spi_mem_op *o
static bool mchp_coreqspi_supports_op(struct spi_mem *mem, const struct spi_mem_op *op)
{
- struct mchp_coreqspi *qspi = spi_controller_get_devdata(mem->spi->controller);
- unsigned long clk_hz;
- u32 baud_rate_val;
-
if (!spi_mem_default_supports_op(mem, op))
return false;
@@ -557,14 +553,6 @@ static bool mchp_coreqspi_supports_op(struct spi_mem *mem, const struct spi_mem_
return false;
}
- clk_hz = clk_get_rate(qspi->clk);
- if (!clk_hz)
- return false;
-
- baud_rate_val = DIV_ROUND_UP(clk_hz, 2 * op->max_freq);
- if (baud_rate_val > MAX_DIVIDER || baud_rate_val < MIN_DIVIDER)
- return false;
-
return true;
}
--
2.47.2
commit e3f1164fc9ee ("PM: EM: Support late CPUs booting and capacity
adjustment") added a mechanism to handle CPUs that come up late by
retrying when any of the `cpufreq_cpu_get()` call fails.
However, if there are holes in the CPU topology (offline CPUs, e.g.
nosmt), the first missing CPU causes the loop to break, preventing
subsequent online CPUs from being updated.
Instead of aborting on the first missing CPU policy, loop through all
and retry if any were missing.
Fixes: e3f1164fc9ee ("PM: EM: Support late CPUs booting and capacity adjustment")
Suggested-by: Kenneth Crudup <kenneth.crudup(a)gmail.com>
Reported-by: Kenneth Crudup <kenneth.crudup(a)gmail.com>
Closes: https://lore.kernel.org/linux-pm/40212796-734c-4140-8a85-854f72b8144d@panix…
Cc: stable(a)vger.kernel.org
Signed-off-by: Christian Loehle <christian.loehle(a)arm.com>
---
kernel/power/energy_model.c | 13 ++++++++-----
1 file changed, 8 insertions(+), 5 deletions(-)
diff --git a/kernel/power/energy_model.c b/kernel/power/energy_model.c
index ea7995a25780..b63c2afc1379 100644
--- a/kernel/power/energy_model.c
+++ b/kernel/power/energy_model.c
@@ -778,7 +778,7 @@ void em_adjust_cpu_capacity(unsigned int cpu)
static void em_check_capacity_update(void)
{
cpumask_var_t cpu_done_mask;
- int cpu;
+ int cpu, failed_cpus = 0;
if (!zalloc_cpumask_var(&cpu_done_mask, GFP_KERNEL)) {
pr_warn("no free memory\n");
@@ -796,10 +796,8 @@ static void em_check_capacity_update(void)
policy = cpufreq_cpu_get(cpu);
if (!policy) {
- pr_debug("Accessing cpu%d policy failed\n", cpu);
- schedule_delayed_work(&em_update_work,
- msecs_to_jiffies(1000));
- break;
+ failed_cpus++;
+ continue;
}
cpufreq_cpu_put(policy);
@@ -814,6 +812,11 @@ static void em_check_capacity_update(void)
em_adjust_new_capacity(cpu, dev, pd);
}
+ if (failed_cpus) {
+ pr_debug("Accessing %d policies failed, retrying\n", failed_cpus);
+ schedule_delayed_work(&em_update_work, msecs_to_jiffies(1000));
+ }
+
free_cpumask_var(cpu_done_mask);
}
--
2.34.1